stephanie51277
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First and formost, thank you all again for everyones ideas and help! I think i narrowed this problem down to an engine problem, not a clutch problem. So i took my 30cc engine all the way out and cleaned it. It has a good amount of dirt on the carb from the gas/oil mixture leaking on it, but i think it is normal leakage because it looked old and im almost positive its been like that for a while, while the truck was in good working order. I also seen that the airfilter had some gas/oil mixture on it that was comming threw the carb, this looks like a new thing since it had made its way threw the two filters and apeared wet in about a dime size area on the outside of the filter that i don't remember seeing befor. The inside of the filter was wet in about the size of a half dollar. Is this normal??? The other thing i noticed was the tune pipe had been smashed about a quarter of the way down in the mid section witch is about a half dollar size. I think this happened in the crash that ultimatly caused my truck to run like crap. To re cap the crash... I jumped it, landed crooked, and it cartweeled and rolled violently. When i fliped it back over, the engine reved but the truck didnt move. Thats when i took the center diff off, didnt see anything wrong, put it back on and the truck would only run at half speed, even going down hill the engine would only get half r.p.m.'s and the clutch bell was red hot after only 2 or 3 min of running. After that first test run i noticed the tune pipe was out of the holding bracket at the end of the pipe, this is why i think the damage on the pipe happened in the crash. Also the gasket that is in the middle of the tune pipe is shot, i think it has been this way for a while but not sure. The truck is pretty new, only about 10 tanks or so ran threw it. When i blew threw the damaged pipe, it didnt apear to have any resistance. Could this be my problem??? Or the gasket, or combination of both??? Also the 2 bolts ataching the pipe to the engine were really hard to get off, one a little more than the other. So much that i unscrewed them only half way scared that i wouldnt be able to get back on if i took them out all the way, is this normal??? The gasket between the pipe and engine apeared to be good and so did the seal once i tighted the bolts back on. Thank you to everyone and all of the help i have got, i think im very close to getting to the bottom of this now, and i cant wait to get this truck running again!!!